Bang-cheng HAN, Zan HE, Lu-xin ZHAI, et al. Loss calculation and thermal-structural coupling analysis of a single gimbal magnetically suspended control moment gyroscope[J]. Optics and precision engineering, 2018, 26(10): 2463-2474.
DOI:
Bang-cheng HAN, Zan HE, Lu-xin ZHAI, et al. Loss calculation and thermal-structural coupling analysis of a single gimbal magnetically suspended control moment gyroscope[J]. Optics and precision engineering, 2018, 26(10): 2463-2474. DOI: 10.3788/OPE.20182610.2463.
Loss calculation and thermal-structural coupling analysis of a single gimbal magnetically suspended control moment gyroscope
To investigate the temperature rise caused by loss of the magnetically suspended control moment gyroscope for the spacecraft application
it is necessary to analyze and calculate the loss and temperature distribution. In this paper
theoretical loss models that consider the iron and copper losses were established. The losses in a single gimbal magnetically suspended control moment gyroscope (SGMSCMG)
which consists of a frame torque motor
radial magnetic bearing
axial magnetic bearing
high-speed motor of rotor system
with a rated speed of 12 000 r/m and maximum angular momentum of 200 N·m·s were calculated. These losses were then used to determine the temperature distribution
which was based on a three-dimensional finite-element model. A thermal-structure coupled simulation analysis was also performed. The results reveal that the maximum temperature occurs at the stator of the high-speed motor and has a value of 48.3℃. Finally
the temperature rise of the prototype is verified by experiment. According to the experiments
the maximum temperature occurs at the stator of the high-speed motor
and its maximum value is 51.8℃. The error is 6.8% when the experimental results are compared with predicted values. The loss calculation and finite element analysis of the thermal field are verified by the temperature rise experiment. The experimental results provide theoretical reference for overall structure optimization.
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references
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